Jim.The.STEAM.Clown - AM/PM - 30 - WoHooooo got the motors running
Next Steps:
- I need to look at changing the motors for a higher gear ratio, so they will run slower
- I need to pick a method to sense the edge of the table
- Right now it runs with an Arduino Controller, but I was thinking of adding a Raspberry Pi too
What
jim.The.STEAM.Clown Did Today:
- Mounted the original motors. These may be too low of a gear ratio for a table top bot. They seem to work fine for on the ground.
- I soldered on wires to the motors and then tested that they worked with a 5 V DC power supply. They worked.
- I then connected the motor controller, and tested the Arduino code. I’ll add links later to the Resource page.
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